The bad mojo is gone, and I’m back on track now. Last night, I wrapped up construction of the top, in spite of it being 50 degrees in the shop. I know I know I’m a big sissy; but I like to be warm, when I’m working in the shop. It’s kind of hard to focus on the task and hand, when you keep pondering what temperature frostbite start to become a concern.
The first thing I did, and forgot to take a picture of, was crosscut the tops to length. Routing holes for the dishes, was the second and most time consuming step of the evening. While it’s time consuming, it’s simple with a router circle jig. Step one is to locate and drill the hole for the centering pin. Step two is to pick the appropriate radius, and the final step is to start making saw dust.

Applying double sided table to the bottom of the top.

Ready to rout the holes
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After Today, I think I’m going to avoid the shop for a few days. I have some bad mojo hanging over my head, because last night I did something I almost never do. I broke the cardinal rule of woodworking; measure twice, cut once. When I purchased the wood for this project, I picked up a beautiful 12″ wide board so I could make the top out of one piece. Last night, everything started out smoothly. I ripped the board to length, flattened it, and jointed an edge in short order. When it came time to rip it to width, I wasn’t paying attention, and read the fractional part of the measurement of the length line on my scratch pad. Thus I ripped it to 10-1/8″, instead of 10-11/16″.
Thankfully I had enough extra stock that I could fix the problem. Thus after much cursing & pouting, I fixed my blunder. I ripped the top into 2 narrow piece, and then added a 3rd board milled from the extra stock. While it doesn’t look that bad, it’s not as nice as it could have been.
Remember: measure twice, cut once.

John Economaki over at Bridge City Tool Works recently published a blog post titled $5 for a 1/8? Twist Drill? Only in America… (it’s a great read). I won’t spoil it for you, but during his tour of a Chinese factory a worker tells John “In America, if it cost less than $20, nobody complains about quality—everybody in China knows this”.
Today I Purchased a new smoother from eBay. It’s a Stanley #4 type 14 that I picked up for $19.99. It only has two things wrong with it that I can see; The lever cap is not original, and the tote is broken (easily fixable). Even if it shows up with a defect that makes in unusable, I can still sell the parts on eBay and make more than I paid for it. Thus, I can promise this is one purchase I won’t be complaining about.
Day for went a little slower than day 3, but I still made A great deal of progress. I started off by finishing the apron pieces, all I had left to do was rout the button grove. The groves are 5/16″ of an inch deep by 1/4″ wide. That’s to much material to remove in one pass, so I took 5 1/16″ deep passes. The groves came out Ok, but if I feed to fast, they router bit complained.

The button grove
What really consumed a lot of time was the next step, tapering the legs. This is the first project I’ve incorporated tapers into. It took a lot longer than I though it would, to get the jig set up correctly. Eventually, I got everything dialed in and was able to batch out the legs fairly quickly. One thing I need to remember for next time, is to not use an 80 tooth cross cutting blade. While it left an excellent finish, my little contractor saw was working really hard to make the cut.

Tapering the legs on my new tapering jig.
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I got a lot more done on day three of this project, than I have in any previous project. I attribute the increased efficiency, to my new router table. Since the pieces for this project are small, it’s safer and faster to rout them on the table, than by hand. Day three started at the table, by making the stopped sliding dovetails in the legs. One thing worth noting, is that the dovetails, are 1/2″ wide, but I used a 3/8″ bit to make them. This requires 3 passes, One down the middle to remove the bulk of the material, and then one down each side, to bring the tail to the final width. It takes longer than using a bit of exact width needed, but in my opinion it produces a superior joint. Passes two and three, remove very little material, and are thus less likely to produce chatter, & inaccuracies.

A raised stop block promotes accuracy, think about it.

Loving the new inserts
Next I cut the mating dovetails in the apron ends. Again, multiple passes are better than one. In this case I used two passes, One that just nicked the surface to prevented tear out, and one that brought the tail to final width. To support the boards while routing, I used my favorite jig. Ok, not really I bug through the scrap bin till I found a decent sized piece of MDF, and then I straitened & squared two of it’s edges.

Multiple passes prevent tear out

Scrap MDF makes a perfect jig for controll tall narow boards.
With the dovetails done, it was on to the table saw to cut the haunches. Yes I said haunches, square blocks don’t fit in round holes. The bottom of the leg tails are round (a side effect of using a router), and the apron tails are square so something has to give. Now I could round over the apron tails with a file, or square the leg tails with a chisel, but that’s to much like work. After they’re glued up no one will know what method I chose anyway. As you can see in the following photos, I morphed into David Marks, and used my cross cut sled just because I could. Continue Reading…